Loading...
HomeMy WebLinkAboutTschiggfrie Excavating Co-11/22/2010 (2)CITY OF WATERLOO, IOWA CHANGE or EXTRA WORK ORDER NO. 1 PROJECT: F.Y. 2010 RAINBOW DRIVE AND LETSCH ROAD FORCE MAIN CONTRACT NO. 792 Date Prepared: November 8, 2010 AMOUNT: $1,973.26 INCREASE TO: tSCHIGGFRIE EXCAVATING CO. , Contractor You are hereby ordered to make the following changes from the plans and specifications or perform the following extra work on your contract dated September 27, 2010. A. Description of change to be made or extra work to be done: Adjust original construction quantities to actual construction quantities. B. Reason for ordering change or extra work: As -built quantities varied for some bid items. C. Settlement for cost of work to be made as follows: Compensation already made to contractor through original bid items. See attached summary. NET INCREASE $1,973.26 CITY OF ATERLOO L/ ' , BY: � / r !AO 1 HIGGFRIE EXCAVATING CO. Mayor Date CONTRACTOR BY: Change Order No. 1 PRINTED NAME: TITLE: S //j& APPROVED: Date /11/510 City Engineer Date Contract No. 792 Page 1 of 1 F.Y. 2010 RAINBOW DR./LETSCH RD. FORCE MAIN -- CONTRACT NO. 792 QUANTITY ADJUSTMENTS BID _____ TSCHIGGFRIE PLAN FINAL INCR/DECR INCR/DECR ITEM DESCRIPTION UNIT UNIT $ QTY. QTY QTY -- AMOUNT 1 FORCE MAIN, 8" DIA. LF $84.68 950.0 971.0 21.0 $1,778.28 ___2 _BEND, 22 1/2 DEGREE, 8" DIA. EACH $329.53 1.0 1.0 0.0 3 BEND, 45 DEGREE, 8" DIA. EACH $334.53 $0.0_0 _ 2.0 2.0 0.0 $0.00 4 LONG PATTERN SLEEVE, 8" DIA., M.J. EACH $359.53 3.0 1.0 (2.0) 5 TAP AND COLLAR STRUCTURE EACH $1,025.00 1.0 1.0 0.0 ($719.06) 6 REMOVE EXISTING STRUCTURE, SANITARY MANHOLE EACH $810.00 1.0 0.0 (1.0) _$0.00 ($810.00) 7 ABANDON EXISTING FORCE MAIN LS $2,316.00 1.0 1.0 0.0 $0.00 8 REMOVE/REPLACE MISC. PCC PAVEMENT, 8 1/2", M-4 SY $75.04 135.0 90.4 (44.6) ($3,346.78) 9 REMOVE/REPLACE MISC. HMA PAVEMENT, 7.5" SY $123.23 90.0 143.7 53.7 $6,617.45 10 REMOVE/REPLACE MISC. PCC CURB AND GUTTER, 24" X 7.5" LF $74.16 30.0 20.0 (10.0) ($741.60) 11 DRAIN TILE, 4" LF $15.01 30.0 8.0 (22.0) ($330.22) 12 GRANULAR SUB BASE TON $27.93 75.0 58.0 (17.0) ($474.81) 13 TRAFFIC CONTROL _ LS $3,400.00 1.0 1.0 0.0 $0.00 _ TOTAL INCREASE $1,973.26 ORIGINAL CONTRACT AMOUNT $116,065.13 CHANGE ORDER NO. 1 - QTY ADJUSTMENTS $1,973.26 FINAL CONTRACT AMOUNT $118,038.39 PAYMENTS TO CONTRACTOR ESTIMATE NO. 1 $112,136.47 RETAINAGE $5,901.92 TOTAL PAYMENTS TO CONTRACTOR $118,038.39 11/8/2010 Page 1 7921NCR-DECR.xls